For the next few weeks not much is going to be happening, as it turns out the panel shop is having an extension to their workshop done this week and I have exams approaching, so we have decided to push the work back another week so they don't have to push the car in and out of the workshop and they can just leave it in there to work on it..
This means I have a week to see if I can get it running..
I have done a bit of looking around and it seems the previous owner swapped the ignition switch out to a 68 / 69 switch..
At least now I know what I need to get it to start.... Hopefully!
If it's not the switch and there's no visible damage to the wires, what else can I look at?
I heard the solenoids often play up, what can I test there?
The only thing I did to is was when I took the wires off it when I hid the wiring harness under the fenders, but I labelled each one of them carefully and have triple checked they are all in the correct spot again..
But this is where I really need some advice! As I have previously mentioned, it's been running on quite badly for anything up to about 15 seconds (which feels a lot more like a minute or two) before finally cutting out.
I have noticed however that it only wants to run on when it's been running for about 5+ minutes, anything less than that when it doesn't get to operating temperature and it doesn't seem to happen as frequently or at all!
The carby has been sitting on the shelf for about 2 years while the engine was out, so I am certain it's tuning has slipped, and that's before I've been messing with it.
I've tried resetting the curb idle speed, idle speed and fuel mixture with some basic (and generic to "single barrel carburettors") instructions I found online so they weren't particularly useful, although it did get it running marginally better.
The automatic choke is not working as there is no pipe to the extractors to operate it, which of course doesn't help..
I know I haven't got the carby tuned properly and it has been running like a dog at idle, although out on the road it seems to run better.
I'm almost certain it's the mixture that is doing it, because I've had a timing light on it and the timing is now set properly (almost perfect actually!) and while I did swap out the spark plugs, they were matched to the old ones perfectly. It's running regular unleaded.. Which was what it had before I took the engine out and all the problems arose.
It's only a little 1BBL Holley and I can't find much on how to tune it properly because everyone swaps to a 2BBL (350 or 500CFM), is there anyone who can offer some good advice on how to get it tuned back to stock settings so it stops running on?
Can anyone recommend a workshop that will be willing and is able to tune it properly, do a roadworthy check and do any remedial work then give it a roadworthy?
Someone on the north-west side of Melbourne is preferable.
It's good to know at least that everything that has gone wrong is because of something I did!
It means it shouldn't be too hard to figure out and it also means it's not something that has gone horribly wrong!
I'm sure when I do I'll be kicking myself I didn't find it sooner!